Twin turbo 4V - 1996 Mustang Cobra

1996 Mustang Cobra with HP Twin turbo kit
This site is dedicated to my 1996 Cobra and follows the installation of a HP Performance twin 57 mm turbo kit.
Read the installation summary here, see below for quick updates.

UPDATES:

03/09/2010 09:27 PM

 

I haven't touched the site or the car in a while, but I wanted to tell everyone about a company I found that makes great products for do-it-yourselfers. If you don't have a lift (like me), these are a must!

MechaniComfort

I have the wedge headrest, the mat and the knee pad and honestly I can't work on my car without them.


12/29/2007 07:05 PM

 

This is a little late, but still worth posting. Back in September I brought the car to the NMRA race in Columbus, OH and entered it in the True Street competition. Here's a video of the best pass of the weekend, a 12.80 @ 111. Launching the car was tricky... too much gas and the tires spun, not enough and the engine bogged. I managed a 2.05 60' time depsite the stock suspension and 3.27 gears. There's no doubt in my mind that an upgraded rear suspension would do wonders.

NMRA Columbus Video

I honestly thought the car would do better than a high 12 at 111, but I think the lack of traction in the first 60 feet really hurt the 1/4 mile time. The full Griggs setup with Torque Arm and Panhard bar should help plant the rear end the next time out.


04/27/2007 04:02 PM

 

Since the weather has been bad this spring there's not much to update.  Even so, there have been a few nice days on which I've been able to drive the car some and it feels great for the measly 4 PSI I'm pushing through the engine right now.

I'm still planning on have the Don Lasota finalize the tune and when I do there will be plenty of pictures and videos posted.


01/02/2007 07:56 PM

 

My stint in Canada lasted just shy of 3 months so I haven't had the time to update the site or update the car.  Needless to say it hasn't seen a dyno yet, but I am confident in the tune and I have been driving the car.  Last week I gave a couple friends a ride and one of them had a camera...

Click here for the video


10/29/2006 08:53 PM

 

Well, I've been up in Canada for 18 of the last 21 days so progress on the car has almost ground to a screeching halt.  I had a chance last weekend to take a few pictures of the car and do a little tuning.  I leaned out the idle and part throttle but still have slight problems with both.  I'll rely on the experts at LaSota Racing (www.lasotaracing.com) to help me iron those out.  More importantly though I got a chance to do some wide open throttle tuning.  I now know why those O2 sensors were so black.  The MAF TF was off causing the car to be incredibly rich at wide open throttle.  I think the worst I saw was 9.3:1!  It's no wonder I thought I had spark blow-out at ~4000rpms at part throttle.  There's no doubt in my mind that the ECU was drowning the spark with fuel.  This is pretty much a tease though, because I don't have any videos or sound clips or dyno numbers.  However, I can tell you  that the car has a ton of power, well, at least it feels like it to me.  At 3.8 PSI I'm impressed and can't wait to turn up the boost a little.

I still have some things I need to wrap up before phase one of the build is complete.  I need to get the tailpipes bent to allow more clearance for the wheels, have an exhaust shop close up my open wastegate vents (I'll have them route it back into the downpipe), install a water temp gauge, and, of course, get together with Don and Rob of LaSota Racing and finalize the tune.

Here are some pictures I took on Saturday, October 23.  Click them for the high-res (2816x2120) versions.  In some of them you can see the wideband O2 wire and connector dangling below the driver side exhaust.

 


10/16/2006 09:13 PM

 

As I said earlier I thought I had an exhaust leak based on the logged fuel trims.  My short term fuel trims were not within 5% of each other and at times they were outside of 10% of each other.  Generally they should be within 5% and if they aren't a few things could be the cause.  One is an exhaust leak, but with all of the exhaust clamps tight I questioned that line of thinking.  Especially since the driver side O2 sensor was showing odd behavior in all of the logs.  This led to me to believe that I had a bad O2 sensor on the driver side (Bank 2).  Luckily my family has another Cobra on hand for times like these.  I took the Bank 2 front O2 out of the other cobra, put it in the vert and started it up.  Amazingly the slight miss was gone and the log showed a functioning Bank 2 front O2.  I immediately ordered 2 new front O2 sensors.  Afterwards I realized that I could have just swapped the O2s from right to left.

When I took the O2 out of the convertible and compared it to the other Cobra's O2 this is what it looked like:

One guess as to which one came out of the turbo car.  I guess the oil and ridiculously rich condition took it's toll on this bad boy.  The plugs look good though.


10/15/2006 04:59 PM

 

NEW WHEELS!

I've wanted these 10th Anniversary Cobra wheels for a while now and I got a screaming deal on them with tires.  My biggest concern was tailpipe clearance because the stock wheels were very close to hitting the Bassani pipes and these wheels are an inch wider.  They fit, barely, and it took a 1/2" spacer to keep the tires from hitting the tailpipes.  Here they are:

 


10/12/2006 07:51 PM

 

The Brake Saga

The original plan was to put the 500 miles of break-in on the clutch and then have it tuned.  I hit the 500 miles in late September,  I think it only took me a week and half of driving to do it.  While I was driving around I noticed that during braking from ~60 mph the car shook violently.  Of course I was eager to get the car tuned but I sure as hell didn't want to go through the embarrassment of telling my tuner that, "um well, the brakes shake, but we'll just have to deal with it."  So I ordered Brembo replacement rotors and Hawk HPS pads.  I have this setup on another car and it stops... in a hurry.

On October 2nd I changed the brakes and my plan was to get the car tuned that Thursday.  I finished everything up at about 10 pm and took it for a spin to make sure I had everything buttoned up.  To my dismay I heard a dragging sound coming from the rear of the car and under heavy braking there was a clunking sound coming from the front.  Back to the driveway it went.

Remember this piece:

It was seized so we bought a replacement from NAPA.  At first the guy at NAPA ordered the whole caliper, but we didn't want to pay for all of it so we asked if he just had the bracket.  He did, we got it, and put it on.  BUT we found out on Monday, October 2nd that he ordered the wrong part.  When we took the wheel off of the passenger side rear we noticed that the bracket wasn't wide enough for the rotor.  After a few minutes of scratching our heads and wondering how that could be I remembered that GT brake rotors aren't vented and are therefore thinner than the Cobra vented brakes.  The old rotor was thin from wear so it fit with the GT bracket!  We grabbed the old rotor and put it back on.  Later that week I stopped by a local Ford dealership and ordered the correct caliper bracket.

Wait, it gets even better.  The new caliper bracket arrived from Ford on Friday, October 6.  I've been out of town since that morning so Dad went to the dealership and picked it up for me.  Everything was going fine until he went to put the screws in the pins (the top two in the picture above).  They wouldn't thread into the hole.  The NAPA piece came with its own screws and they're different threads than the stock Ford piece!  Unreal.  The last I heard was that Dad found the right screws at a hardware store.

The front brakes are still a mystery.  Under light braking we don't notice any noise, but under hard braking it almost sounds like something is loose.  It's odd because the clunking sound follows the wheel speed.   We went over every nut and bolt that we could think of and none of them are loose.  I don't know what to do.

Needless to say I'm not going to be doing any WOT blasts with questionable brakes, so the car remains untuned.  The good news is the stock bottom end is still together.


09/21/2006 10:53 AM

 

I drove the car to work today.  I'm really happy with the way it's running right now.  The break-in procedure for the clutch says no WOT for the first 500 miles, which is good anyway because the car doesn't have the final tune yet. Not mashing the throttle has been difficult, but I have seen about 3 psi at half throttle and it felt pretty damn good. The blow-off valves sound awesome. At half throttle it's 12:1 so I think I'm safe enough there until I get the full tune. It rides like stock once you get going, but the idle is just a little bit off. I think there's a slight miss but it's not very noticeable.  All in all I'm happy with the way it is right now.

I still need to get in touch with the Lasotas at Lasota Racing in Columbus, Ohio.  Don will be doing the tuning and he's got a great reputation.  If you have a chance check out their website at www.lasotaracing.com.


09/18/2006 12:12 PM

 

The oil problem has been fixed!  Rotating the turbos so that the drain was straight down and re-routing the driver side drain line fixed the oil drain back-up.  I took the car for a long ride last night and didn't notice any smoke.  I need to log the fuel trims to see if the exhaust leak is still there.  We found evidence of a leak on the passenger side and tightened the exhaust clamp in the hopes that it would eliminate the leak.

Finally, the car is driveable.


09/12/2006 03:08 PM

 
A BIG THANKS TO D&D PERFORMANCE FOR THEIR HELP WITH THE T56

As I've documented I contacted D&D Performance about the crack in the tailhousing.  To be honest I was little worried about having to pay for the new tailhousing.  As it turned out I didn't have to.  D&D went above and beyond the call of duty by replacing this part for free.  I spoke with Don Walsh Sr. at the NMRA Atco race and the NMRA Columbus race and his wealth of knowledge and approachability are impressive.  We spoke for about 20-30 minutes about the differences between the mustang transmissions over the last few years and I really appreciated the conversation.  In fact, when I called him between races about my speedo gear being incorrect he said he'd bring one to the Columbus event and sure enough when I stopped by on Sunday he had one there waiting for me.

Thanks for the help Don Walsh Sr. and to all of those reading this go to www.ddperformance.com and checkout what D&D has to offer.  They are definitely THE place to go to for transmission upgrades.


09/12/2006 02:54 PM

 

The car sat in my garage untouched for almost a week.  On Labor Day, September 3, 2006, I drove the car over to my parents and put it halfway inside their garage.  It smoked, pretty badly at times, out of the driver side tailpipe.  There's no doubt that the oil drain line on the driver side needs to be rerouted, the turbo drain flanges need to be rotated, and the exhaust clamps needed to be checked for signs of leakage.  We're also going to investigate crankcase pressure build-up preventing adequate oil draining.  If we find that it's a problem we'll have to redo the crankcase vent.  Right now it goes from the passenger side valve cover to the passenger side air filter and the driver side is stock.

Finding these problems and applying solutions might take a while.  The car will remain parked until we stop the smoking and fix the exhaust leak.


08/31/2006 09:23 AM

 

Well, the tailhousing arrived last week and we installed it on Sunday.  It was raining off and on so I only got to take the car for a short drive afterwards.  The tune still needs some work, so I've kept it under 4 PSI and 4000 rpm but I'm impressed.

I got the car home Tuesday night and did about 70 miles of driving along the way (took a long detour to help out a local stanger).  The driver side smokes badly.  I think we have oil drain line issues on the driver side.  I'm sure there is a low spot in the line that caused the back-up.  I'm also going to look into a feed line restrictor to keep too much oil from flowing into the turbo housing. The oil issues need to be solved before any significant driving is done because they could lead to blown turbo seals and a turbo rebuild...

I finally figured out what was wrong with the Xcal 2 / Livelink.  I was using a configuration for the 97 and it was causing problems.  I made a new configuration Tuesday night and it worked flawlessly.  The datalog indicated that we have an exhaust leak.  While we are working on the drain lines I'll go over all of the clamps and see if I can find the leak.  I hope it's not between the header and the head...


08/25/2006 11:59 AM

 

The tailhousing showed up yesterday.  I'll install it this weekend.  If everything goes as planned I'll be putting the 500 mile break-in on the clutch next week and then it's off to the tuner for some WOT fun.


08/19/2006 07:59 PM

 

On Tuesday night we took the T-56 out of the car.  We were able to get the transmission out of the car and the tailhousing off in less than 3 hours.  I honestly thought we would have been working a lot longer than that.  D&D is sending a new tailhousing, it should arrive next week sometime.


08/15/2006 12:53 PM

 

On one of the Mustang forums a while back I was complaining a little bit about a few problems I've encountered along the way.  One guy responded with: "That's hot-rodding get used to it."  Well, whether or not I'm used to it, it certainly is hot-rodding.

Last Tuesday the car got aligned.  The guys at the alignment place said it was almost perfect, but the car was so low that they ran out of caster adjustment on the Maximum Motorsports caster camber plates.  Close was good enough, I just wanted to drive the thing.

Before I did anything I wanted to get some datalogging done so I could be sure that the tune was safe enough.  Unfortunately I couldn't get the SCT Xcal 2 to keep communication with the LiveLink datalogging software.  I called SCT and they kindly pointed out that I did not have the latest version of LiveLink.  Lesson learned: SCT does not update the forums with the latest software.  The latest software is only available in the downloads section.  At any rate, the car was low on gas so we decided to run up to the gas station and fill her up.

When we got back I took the wideband O2 out of the driver's side exhaust and noticed this:

The T-56 tailhousing has a crack in it.


08/03/2006 09:52 AM

 

The T-56 is in the car, we had some time on Tuesday night to finish up the transmission mount, but as we were putting the exhaust back on we noticed that the downpipe was hitting the oil filter.  I ordered an oil filter relocation kit from Maximum Motorsports yesterday and I got the expedited shipping so it should be here by Friday evening.  Also, I figured out why the SCT Advantage software would not communicate with my Xcal 2 (hint: keep your software updated).  With some luck I should be able to fire the car up this weekend and let it idle without doubling over from the raw fuel in the exhaust.

My tranny rebuilder had time to look at the internals of the T-45 and noticed that he put the 1-2 shift plate in backwards.  Live and learn, we now know that everytime you rebuild a tranny you should put it in each gear, rotate the input shaft, and count the output shaft revolutions to make sure you did it correctly.  It's not really a big deal though, that transmission was a ticking timebomb with this setup anyway.  Now I have a transmission that I don't have to worry about.


07/26/2006 01:03 PM

 

The T-45 is out, and hopefully we can install the new DFX clutch disc and the T-56 this weekend.

I added the May 7, May 13 and 20, and May 26 write-ups, along with updating the To Do List


07/10/2006 10:07 AM

 

We fixed the fuel leak and started the car but we've got more problems.  The base tune was off and the car was incredibly rich, so rich in fact that we couldn't let the car run for more than a few seconds while in the garage.  It didn't take long before our eyes were burning and we were having trouble breathing even with the garage door open and fans running.  So we put the car on the ground and tried to move it outside.  The first thing I noticed was how difficult the shifter moved into gear.  When I tried to move the car forward the transmission felt like it was still in 3rd gear.  I moved the car outside and drove it up and down the driveway and was sure that something was wrong.  Originally we thought the clutch was not adjusted correctly because we hadn't received the adjuster from the Modular Depot, but upon investigating further we ruled out the clutch.  That leaves the transmission and if you remember when I broke the transmission back in the fall it wouldn't come out of third gear.

So we're going to tear it down again, remove the T-45 and replace it with a Viper spec T-56 that I just purchased.  I'll also need to upgrade the clutch disc to a 26 spline unit and I'll make sure I get the DFX clutch this time.  So completion of the project has been delayed yet again.


06/26/2006 12:24 PM

 

We tried to start the car yesterday but couldn't because of a fuel leak at the regulator.  We figured out the problem and should have it fixed and running soon.

To Do List


06/13/2006 02:41 PM

 

I decided to not use the pyrometer and gauge and also decided on my front O2 extensions.  I'll modify an old MIL eliminator to work as an extension.

Updated the To Do List.


06/12/2006 09:10 PM

 

The shipment arrived from Inline Motors on Tuesday with the GSS342 in it.  Third times the charm...  I also got the lower spring perch and sleeve from Maximum Motorsports.

Saturday I installed the pump, tank, finished the front suspension (minus ride height adjustment and alignment), and test fit the exhaust.  Here's what's left to do.


06/06/2006 01:12 PM

 

Unbelievable!  When I opened the package from inline motors on Saturday morning this is what I saw.

The part number was GSS341.  I couldn't believe they sent the wrong pump again.  I finally reached them on the phone Saturday afternoon and they agreed to overnight the right one on Monday.  The package arrived today so I'll be able to check it out tonight.  Hopefully they got it right this time, otherwise I don't know what I'm going to do. 

The Maximum Motorsports package arrived today too.  It should contain a new lower spring perch for the front coil-over setup.  If all goes well the build could be completed this weekend.


05/31/2006 10:29 PM

 

I got a tracking number from inline motors so hopefully they put the right pump in the box this time.

I also talked to Maximum Motorsports and they're sending a new spring perch.  I'm hoping that it and the pump show up by Saturday so I can continue the installation this weekend.  I'm not sure if the exhaust has shipped yet, but Mustang Racing Technologies said it was supposed to ship yesterday (Tuesday).

I also added some more updates to the installation write-up.  The April 15th summary, Finishing the Drivetrain Installation and Remounting the Turbos (1) and Finishing the Drivetrain Installation and Remounting the Turbos (2) are now up.


05/29/2006 10:07 PM

 

More setbacks.  Before this weekend I thought there was an outside shot that I'd be able to fire up the car on June 4th.  Due to some uncontrollable mishaps I don't think that will be a real possibility.  Against my better judgment I bought the Walbro 255 lph fuel pump part #GSS342 on Ebay.  Inlinemtors sent the wrong pump, I received and installed pump #GSS340 and only noticed it in the picture below (hard to see in these low res versions I put up on the site).  Who knows, maybe that pump would have worked but I'm not taking any chances.  I'm going to overnight the pump to him and ask for the correct one to be here by Friday so I can install it on Saturday.  I'm keeping my fingers crossed.

The other problem involved the front coil-over kit from Maximum Motorsports, a company I definitely did not think I would have a problem with.  However I could not get the bottom spring perch to thread onto the sleeve on the front coil-over kit.  The driver side went on perfectly but the passenger side assembly didn't, the sleeve would not thread out of the top of the perch so I'm going to call them tomorrow.


05/29/2006 09:08 PM

 

I added more pictures, pictures page 9, page 10 and page 11 have the newest pictures as of Friday May 26.

I've done some research into turbo drain line routing and everything I've seen has said no low spots and put the drain at the lowest point of the center section.  Take a look at the picture below and let me know if this drain is too far from the lowest point of the center section.  I think it's at about 45 degrees.  Shoot me an email with your comments.

driver side turbo drain line

To be honest we didn't really see any other way of routing the drain line.  We put it in just about the only position that would allow the drain line a straight shot to the oil pan without large bends and ridiculously low spots.  We did end up with one low spot and again, I'm not sure if we can get around or how serious low spots are.  I meant to snap a picture of it today but I forgot.


05/28/2006 11:58 AM

 

More updates.  I added 3 pages of pictures, and found some pictures that should have been included before but were left out for some reason.  Pictures pages 5 and 6 have new pictures and I added pages 7, 8, and 9.

I also added the April 9 write-up Starting the drivetrain install.  We were able to get the oil pan back on, and install the new flywheel, clutch disc, and pressure plate; and we finished up the day by nearly completing the transmission install.

And I updated the part list to reflect everything I have received or at least ordered as of today.

On Friday I ordered the Bassani catback and the Fiore adjustable clutch quadrant.  The only thing left to get is a pyrometer sensor (I already have the gauge).


05/26/2006 12:08 AM

 

Time flies, especially when you have a full-time job, are coaching junior high lacrosse, and trying to build a twin turbo mustang.  I finally had some time to add a little bit of content.  Click here for the March 18 write-up: Tackling the Rear suspension (Part 3)

As you can guess we're a lot further along than I've had time to update.  As of today the oil pan has been welded and installed, the flywheel, clutch disc, and pressure plate have been installed.  The transmission is back in, the turbos have been remounted (and in better spots with more clearance), the drain and supply lines have been connected, the gauges are installed (minus the pyrometer), and I have ordered everything (including the 4 psi wastegate springs) except the Bassani catback.  Hopefully we can wrap things up by mid-June.  Check back for more updates.


05/02/2006 12:41 AM

 

I'm still adjusting to the 12 hour time difference and I couldn't sleep so I added the March 11 write up page 1: "During the week Dad drove over to the local NAPA and picked up the right bolts for the rear control arms.  When we got to..." read more

And I added page 2: "We were ready to dig into the driver side rear suspension and felt that we knew what to do from..." read more


05/01/2006 09:34 PM

 

Well I spent the last week in China for work, fortunately I had time on the plane to work on the site a little bit.  I added some content to the March 4 page 2 write-up.

And I added page 3: "The suspension arrived from Maximum Motorsports in a big brown box a few weeks earlier.  It included..." read more


04/16/2006 09:12 PM

 

I'm finally starting to catch up a little.  I finished the February 18th story.

I also added page 1 of the March 4 summary: "After a one weekend hiatus we were back at it.  With two glaring mistakes behind us we were ready to make some progress..." read more

And I started page 2: "On Saturday March 4, I had, in my hands, a clutch setup that I was happy with and I wanted to install it..." read more

There's a lot more to add to this part of the story.


04/16/2006 11:04 AM

 

I added a picture to the home page and made some buttons for the menu.


04/11/2006 10:18 PM

 

I had some time tonight so I started the February 18 write-up.  I only got about 1/4 of the way through, I'll add more later: "I was away from the install for just over a month because I traveled for work and went on a few personal weekend trips.  On January 21, Dad worked alone and removed..." read more

I also changed the look of the installation page to mirror what I have here on the home page.  I still haven't figured out why the menu doesn't center over the main container in Firefox, it looks perfect in Internet Explorer.  Oh well, I'll figure it out sooner or later...


04/08/2006 06:31 PM

 

I added more pictures, page 5 and page 6 are now up.  Obviously we're a lot further along than I've had time to summarize here.  The transmission is out, rebuilt, and ready to be installed; the stock clutch, pressure plate and flywheel have been removed; and the rear suspension has been installed.


04/08/2006 05:09 PM

 

I had some time today to work on the website... but when I'm working on the website I'm not working on the car.  I added page 4 to the The Weekend of January 14 installation: "Removing the transmission mount should be straight forward.  There are two bolts and two nuts that need to be removed..." read more

And page 5: "While working on the exhaust we talked about our transmission removal options and decided that we would try to lower..." read more


04/03/2006 03:36 PM

 

I've posted links to the site on several mustang forums and have received some feedback.  Using the feedback I made changes to the background page and the home page so that both now include a little bit more information about my intention to complete the project in two steps.  I noticed that a few people asked if the kit was going on a stock short block or a forged short block... the stock rods and pistons will remain in the block until I either blow them to pieces or have the time and resources to build the forged bottom end.  I'm keeping my fingers crossed that they'll be able to survive with 6 psi.


03/30/2006 05:11 PM

 

I finally started The Weekend of January 14 installation.  I added page 1: "When we walked into the garage on Saturday, January 14 we already had our minds made up that we would be installing the turbos and..." read more

Page 2: "Before we could see how sturdy the setup was we had to do a little more metal-work.  We noticed that there wasn't much room between..." read more

And page 3 (even though it is incomplete right now): "The first thing we did Sunday morning was grab the blow off valves, the small blue flexible hose, and some clamps..." read more


03/07/2006 10:41 PM

 

Whew! I can't believe it's been a month since I touched the site.  A lot has changed with the car since I last posted an update: the tranny's out of the car, the stock cat back has been cut-off, I've ordered and received the clutch/flywheel, and the wrong fuel rails.  Right now I have everything but the new cat back, the right fuel rails and the complete fuel system (which is still up in the air, but I think I'll have it nailed down soon).  Tonight I had time to write page 3 of The Weekend of January 7 installation: "While I was busy messing around removing the old exhaust gaskets, my dad was busy cutting up some sheet metal..." read more

And page 4: "Our plan was to slide the k-member over the exhaust flanges on the headers.  We tried going straight up from the bottom, but the k-member wouldn't clear..." read more


02/05/2006 05:03 PM

 

I added page 2 to The Weekend of January 7 installation: "With the stock k-member out of the way we had easy access to the stock headers.  Anyone that has tried to work on a DOHC 4.6 knows..." read more

 Off to watch the superbowl.


02/04/2006 01:04 PM

 

I changed the look of the home page to include a section for my comments and updates.


01/28/2006 08:38 PM

 

I wanted this site to be a way for me to document the installation, but it takes a lot of freaking time to write this stuff.