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January 7-8, 2006 - More Teardown (4)

Our plan was to slide the k-member over the exhaust flanges on the headers.  We tried going straight up from the bottom, but the k-member wouldn't clear the flanges.  So we tried slipping one side over the header first, and swinging the other side into place, but that didn't work either.  The instructions said to notch the k-member on the passenger side, we figured that might just give us enough room to swing the k-member up and clear the headers.  We marked the k-member and started thrashing with the cut-off wheel.  After a few minutes we there was a nice chunk missing and we even took the time to smooth the edges so we wouldn't slice up our hands while putting the tubular k-member up into position.  To our disappointment the notch didn't give us enough clearance to install the k-member over the headers.  Our only option was to remove one header.  Coming to this realization put an end to our night.  We decided that we'd take the passenger side header off in the morning and hopefully we'd be able to move the k-member up to the car, bolt it in place, and install the header without problem.

We got up bright and early Sunday morning and starting undoing our previous work - something we'd get used to.  We took off the passenger side header with ease and I found myself lying on the floor holding a drill with a wire brush attachment flinging permatex off of the head... it felt strangely familiar.  While I worked on the header removal, Dad worked on the sheet metal fab.

With the passenger's side header removed the k-member slid into place with ease. I, however, was left scratching my head as I looked at the amount of room left to squeeze the header back up into place.

When it comes down to it, sometimes you just have to do the job.  So I grabbed the header and started twisting it and turning it. At first it didn't seem like it was going to go up there, but at just the right angle there was enough room for it to slip into place.  I grabbed a 1/4" drive ratchet and sockets and starting tightening the header bolts.  I had to use a universal on a few of them, but it was a lot less painful than I thought it was going to be.  Here's a picture of it installed and torqued to spec followed by pictures of the driver's side header to k-member clearance.

While I was working on the header, Dad was working on the... you guessed it... sheet metal.  So much for that being an easy job.  Well, it probably would have been if someone had stopped burning through the sheet metal and changed the wire to the right thickness, but that didn't happen until there were two huge gaping holes in the sheet metal and Dad was standing there with the wire feed gun in his hand, shaking his head, and saying, "I guess I should have used the thinner wire."  Trust me, it's funny now, but it wasn't then.  We spent the remainder of the day Sunday grinding the heaping weld that we amassed to close the gaping holes burned by someone. Eventually I got bored so I snapped a picture of the twins.   I thought I might be able to cut them out and use them on the website banner...

At somewhere around 7 or 8 Sunday night we called it quits even though there was a bunch more grinding to do.  I think Dad felt bad, because he came out the following Wednesday and finished up the weld removal and painted the sheet metal.  To be completely honest it turned out really nicely, definitely much better than it would have if we had used a hammer to slam the sheet metal around like the instructions said.  I'm not sure which gauge wire you should use if you try to weld the sheet metal on a sn95 Mustang but I'm pretty sure Dad could tell ya.  Here's some before and after pictures of the driver's side sheet metal.

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